FABRICATION AND OPERATIONAL EXPERIENCE WITH THE INTERIM STORAGE CASK

Year
1998
Author(s)
R. M. Grenier - General Atomics, USA
M. A. Koploy - General Atomics, USA
P. L. Scott - B & W Hanford Company, USA
File Attachment
95.PDF1.79 MB
Abstract
This paper discusses the fabrication and operational experience of the Interim Storage Cask (ISC). The ISC is a dry storage cask which is used to safely store a Core Component Container (CCC) containing up to seven Fast Flux Test Facility (FFTF) spent fuel assemblies at the United States Department of Energy's Hanford Site. Under contract to B & W Hanford Company (BWHC), General Atomics (GA) designed and fabricated thirty ISC casks which BWHC is remotely loading at the FFTF facility. BWHC designed and fabricated the CCCs. As of December 1997, thirty ISCs have been fabricated, of which eighteen have been loaded and moved to a storage site adjacent to the FFTF facility. Fabrication consisted of three sets of casks. The first unit was completed and acceptance tested before any other units were fabricated. After the first unit passed all acceptance tests, nine more units were fabricated in the first production run. Before those nine units were completed, GA began a production run of twenty more units. The paper provides an overview of the cask design and discusses the problems encountered in fabrication, their resolution, and changes made in the fabrication processes to improve the quality of the casks. The paper also discusses the loading process and operational experiences with loading and handling of the casks. Information on loading times, worker dose exposure, and total dose for loading are presented.